船东代表检查舾装件后的意见(中英文)

甲板栏杆立柱与甲板的焊接处存在虚焊,用力晃动时可见明显缝隙,不符合 SOLAS 安全要求。There is a cold weld at the joint between the deck railing column and the deck; a visible gap app...
  • 甲板栏杆立柱与甲板的焊接处存在虚焊,用力晃动时可见明显缝隙,不符合 SOLAS 安全要求。
    There is a cold weld at the joint between the deck railing column and the deck; a visible gap appears when shaken forcefully, failing to meet SOLAS safety requirements.
  • 货舱通风筒的防雨帽铰链损坏,无法完全闭合,在模拟降雨测试中出现雨水倒灌现象。
    The hinge of the cargo hold ventilator’s rain cap is damaged, preventing full closure; rainwater backflow is observed during the simulated rainfall test.
  • 舷梯踏板防滑纹路磨损严重,实测摩擦系数为 0.3(设计要求≥0.5),存在人员滑倒风险。
    The anti-slip 纹路 on the gangway steps is severely worn; the measured friction coefficient is 0.3 (design requirement ≥0.5), posing a slip risk for personnel.
  • 机舱内燃油管系的支架间距超标,设计要求 1.5m / 个,实际达 2.2m,导致管路存在明显下垂(挠度约 15mm)。
    The spacing of the fuel pipe supports in the engine room exceeds the standard; the design requires 1.5m per support, but the actual spacing is 2.2m, causing significant sagging of the pipeline (deflection approximately 15mm).
  • 压载水管路的弯头处存在壁厚减薄,实测最小厚度为 5mm(原始厚度 8mm),怀疑是长期冲刷腐蚀所致。
    Wall thickness reduction is found at the elbow of the ballast water pipeline; the measured minimum thickness is 5mm (original thickness 8mm), suspected to be caused by long-term erosion corrosion.
  • 蒸汽管法兰垫片老化硬化,在热态运行时出现微量泄漏,接触式测温显示法兰边缘温度较正常区域高 10℃。
    The steam pipe flange gasket is aged and hardened; slight leakage occurs during hot operation, and contact temperature measurement shows the flange edge is 10℃ hotter than the normal area.
  • 艉尖舱舱壁因吊装碰撞出现局部凸起,变形量达 25mm,超出规范允许的 10mm 限值,可能影响舱容精度。
    The stern peak tank bulkhead has a local bulge due to hoisting collision, with a deformation of 25mm exceeding the 10mm limit specified in the code, potentially affecting tank capacity accuracy.
  • 上层建筑前端壁在焊接后未进行时效处理,出现波浪形变形,最大起伏量 8mm,导致与相邻舱壁的贴合间隙超标。
    The front wall of the superstructure shows wavy deformation due to lack of aging treatment after welding, with a maximum undulation of 8mm, causing the fitting gap with the adjacent bulkhead to exceed the standard.
  • 甲板货舱口围板垂直度偏差,实测垂直度为 15mm/m(允许值≤5mm/m),可能导致舱口盖密封不良。
    The hatch coaming of the deck cargo hold has a verticality deviation; the measured verticality is 15mm/m (allowable value ≤5mm/m), which may cause poor sealing of the hatch cover.
  • 船底牺牲阳极块剩余重量仅为初始重量的 30%(设计更换阈值为 50%),防腐效果显著下降。
    The remaining weight of the hull sacrificial anode block is only 30% of the initial weight (design replacement threshold is 50%), resulting in a significant decline in anti-corrosion effect.
  • 压载舱内阴极保护系统的参比电极读数异常,显示保护电位为 - 0.7V(要求范围 - 0.85V 至 - 1.1V),存在局部腐蚀风险。
    The reference electrode reading of the cathodic protection system in the ballast tank is abnormal, showing a protection potential of -0.7V (required range -0.85V to -1.1V), with a risk of local corrosion.
  • 船体与阳极块的连接电缆绝缘层破损,万用表检测显示绝缘电阻为 0.5MΩ(标准要求≥10MΩ),导致电流损耗。
    The insulation layer of the connecting cable between the hull and the anode block is damaged; a multimeter test shows an insulation resistance of 0.5MΩ (standard requirement ≥10MΩ), causing current loss.
  • 机舱内高压油管未按要求张贴 “高温危险” 警示标识,仅用手写标记且模糊不清,不符合 IMO 标识规范。
    The high-pressure oil pipe in the engine room is not labeled with the "high temperature hazard" warning as required; only a handwritten mark is present, which is unclear and fails to meet IMO marking specifications.
  • 救生筏存放架的承重标识错误,实际最大承重 500kg 却标注为 800kg,存在超载坠落风险。
    The load-bearing label of the life raft storage rack is incorrect; the actual maximum load is 500kg but marked as 800kg, posing a risk of overload falling.
  • 货舱内分隔舱的舱壁未标注限载吨位,船员反馈曾因误判装载量导致局部结构轻微变形。
    The bulkhead of the cargo hold compartment is not marked with the load limit tonnage; crew feedback indicates that minor deformation of the local structure occurred due to misjudgment of the load.
  • 锚链链环存在多处磨损,实测最小直径为 68mm(原始直径 76mm),超过允许磨损量(8%),强度下降约 15%。
    Multiple wear points are found on the anchor chain links; the measured minimum diameter is 68mm (original diameter 76mm), exceeding the allowable wear (8%), with a strength reduction of approximately 15%.
  • 锚机刹车带磨损不均,局部厚度仅为 3mm(标准要求≥5mm),在锚链回收测试中出现刹车延迟现象。
    The anchor winch brake band has uneven wear, with a local thickness of only 3mm (standard requirement ≥5mm); brake delay occurs during the anchor chain recovery test.
  • 锚链管与甲板的连接处密封填料老化,在冲水试验中发现海水沿缝隙渗入锚链舱,导致舱底积水。
    The sealing packing at the joint between the chain pipe and the deck is aged; seawater seepage into the chain locker along the gap is found during the water flushing test, resulting in bilge water accumulation.
  • 发表于 2025-08-19 11:56
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